Post by coniston on Apr 1, 2020 19:45:05 GMT
So I thought I'd start a new dedicated thread for my work on rebuilding a Clarkson 5" A3. First a bit of history. This loco was built by Alan Fay of the Southampton society between 1969 and 1974. A picture reproduced below features on the front of the club newsletter in 1974 in steam ready for leaving the station at SSME track.
I bought the loco from Alan's son a couple of years ago, still complete and operating on air although the last boiler certificate expire in 1999. And here in lies the main problem and reason for a rebuild. The loco was originally built with a steel boiler so re-certification was creating an issue. Unfortunately the original shell test certificates were no longer available having been lost in various house moves, however I did have some of the more recent history. Speaking to boiler inspectors at both clubs I belong to (including Southampton) the conclusion reached was if I could get the original boiler tested by a professional inspector and passed they would be happy to carry out future re-tests. So I took it along to a RSA inspector who tests many traction engine and commercial miniature steam railway loco boilers. Prior to this I stripped the boiler out of the frames and took all fittings, regulator, super heaters off and hydraulic tested it myself to 200 psi just so as not to waste anyone's time. All looked good to start with, the inspector checked inside and commented on how clean and corrosion free it was. next he put the thickness tester on it and that was the problem. The boiler had been made using 10g steel for the firebox inner and outer, this is just not considered thick enough to compensate for corrosion under present guidelines so he had no choice but to refuse to test it. Bit of a bummer but in reality I was expecting to replace the boiler with a new copper one and had made consideration for that.
Wind forward 12 months and I had acquired a copper boiler ostensibly to the Don Young design but with some subtle differences, but at least it did fit the frames. Interestingly there is very little difference in dimensions between Don's Doncaster design and Clarkson's. The big difference is in the level of details and the lack of dimensions on the Clarkson drawings. Oh and Clarkson used slide valves whereas Don uses prototypical piston valve.
Any way I have finally cleared other projects and made a start on the A3, I have some posts in 'what I've done today' which I would love to move to this thread but don't know how, any help much appreciated otherwise please look there for the first instalments.
I'm adding the original posts from 'What I've Done Today thread in here:
1. In the workshop on Sunday actually made a start at getting the new boiler into my Clarkson 5" A3. First job was to make a solid stretcher for the front foundation ring to sit on.
2. Making progress on my A3, made a smokebox ring to increase the boiler to inside smokebox size. Luckily a piece of 10g copper rolled up is just right. Judicial use of a file to get the joint nice and tight then fixed with 6BW CSK brass screws.
Next job is a new ashpan to fit the new boiler. After making a sketch I cut one from cardboard to check the fit. All seemed ok except it touched the rear truck axel. Second version fits nice.
So started cutting metal, I have some 1mm stainless which should be ok for this.
The original one has a hinged middle section, not sure I will follow that as it will be near impossible to clean out under the fixed side sections. My intention is to have the grate in 4 sections sitting either on transverse rods or angles. The bottom will be hinged to allow dropping ash and for disposing of fire.
Hopefully tomorrow I can get the bits cut out and start TIG welding them together.
3. Got another day in the workshop today and yesterday so progress is underway on the A3 ashpan. Mainly milling these to size so I can get them as accurate as possible to help alignment when TIG welding them. Made from 1mm stainless sheet.
Using my ER11 collet chuck which came on a ground 10mm spindle, held in the ER32 milling collet chuck, gets more clearance for the little 3mm throw away cutter.
Couldn't resist taping the bits made so together to check the fit, happy to report everything so far fits nicely.
4. Bit more on the A3 ashpan, got most of the bits made so stated on assembly, just tack welded together to start with. I bought a small, IIRC WP9, torch for my TIG welder, smallest I could get, along with 1mm tungsten electrodes. First time I used it today so I played around on some scrap bits until I got it about right. Much easier with this small torch for thinner gauge metal. Plenty of air holes so hope the fire will burn bright.
5. So today I have almost finished the ash pan, fully TIG welded, some good welds, others done by the overhead pigeons!!. I have made the ash drop door and fitted it using a short length of commercial stainless steel piano hinge, cut down to make it a bit neater. Currently temporarily fixed with 10BA screws and nuts, this will be rivetted finally. Only the door latch to make and fit and then onto designing a grate. Not sure to make 4 piece removable or fixed with hinge down centre part. The former will allow complete cleaning of the ashpan with a vacuum cleaner and brushes, the hinge down one will be fewer loose parts but the fixed sections each side prevent full access to the shallow 'wings' of the ashpan for complete cleaning.
At least it still fits, although there is some distortion I need to take out for a better fit.
And the hinged door being fitted.
Hope to finish off the ash pan tomorrow and scheme out the grate.
Chris D
I bought the loco from Alan's son a couple of years ago, still complete and operating on air although the last boiler certificate expire in 1999. And here in lies the main problem and reason for a rebuild. The loco was originally built with a steel boiler so re-certification was creating an issue. Unfortunately the original shell test certificates were no longer available having been lost in various house moves, however I did have some of the more recent history. Speaking to boiler inspectors at both clubs I belong to (including Southampton) the conclusion reached was if I could get the original boiler tested by a professional inspector and passed they would be happy to carry out future re-tests. So I took it along to a RSA inspector who tests many traction engine and commercial miniature steam railway loco boilers. Prior to this I stripped the boiler out of the frames and took all fittings, regulator, super heaters off and hydraulic tested it myself to 200 psi just so as not to waste anyone's time. All looked good to start with, the inspector checked inside and commented on how clean and corrosion free it was. next he put the thickness tester on it and that was the problem. The boiler had been made using 10g steel for the firebox inner and outer, this is just not considered thick enough to compensate for corrosion under present guidelines so he had no choice but to refuse to test it. Bit of a bummer but in reality I was expecting to replace the boiler with a new copper one and had made consideration for that.
Wind forward 12 months and I had acquired a copper boiler ostensibly to the Don Young design but with some subtle differences, but at least it did fit the frames. Interestingly there is very little difference in dimensions between Don's Doncaster design and Clarkson's. The big difference is in the level of details and the lack of dimensions on the Clarkson drawings. Oh and Clarkson used slide valves whereas Don uses prototypical piston valve.
Any way I have finally cleared other projects and made a start on the A3, I have some posts in 'what I've done today' which I would love to move to this thread but don't know how, any help much appreciated otherwise please look there for the first instalments.
I'm adding the original posts from 'What I've Done Today thread in here:
1. In the workshop on Sunday actually made a start at getting the new boiler into my Clarkson 5" A3. First job was to make a solid stretcher for the front foundation ring to sit on.
2. Making progress on my A3, made a smokebox ring to increase the boiler to inside smokebox size. Luckily a piece of 10g copper rolled up is just right. Judicial use of a file to get the joint nice and tight then fixed with 6BW CSK brass screws.
Next job is a new ashpan to fit the new boiler. After making a sketch I cut one from cardboard to check the fit. All seemed ok except it touched the rear truck axel. Second version fits nice.
So started cutting metal, I have some 1mm stainless which should be ok for this.
The original one has a hinged middle section, not sure I will follow that as it will be near impossible to clean out under the fixed side sections. My intention is to have the grate in 4 sections sitting either on transverse rods or angles. The bottom will be hinged to allow dropping ash and for disposing of fire.
Hopefully tomorrow I can get the bits cut out and start TIG welding them together.
3. Got another day in the workshop today and yesterday so progress is underway on the A3 ashpan. Mainly milling these to size so I can get them as accurate as possible to help alignment when TIG welding them. Made from 1mm stainless sheet.
Using my ER11 collet chuck which came on a ground 10mm spindle, held in the ER32 milling collet chuck, gets more clearance for the little 3mm throw away cutter.
Couldn't resist taping the bits made so together to check the fit, happy to report everything so far fits nicely.
4. Bit more on the A3 ashpan, got most of the bits made so stated on assembly, just tack welded together to start with. I bought a small, IIRC WP9, torch for my TIG welder, smallest I could get, along with 1mm tungsten electrodes. First time I used it today so I played around on some scrap bits until I got it about right. Much easier with this small torch for thinner gauge metal. Plenty of air holes so hope the fire will burn bright.
5. So today I have almost finished the ash pan, fully TIG welded, some good welds, others done by the overhead pigeons!!. I have made the ash drop door and fitted it using a short length of commercial stainless steel piano hinge, cut down to make it a bit neater. Currently temporarily fixed with 10BA screws and nuts, this will be rivetted finally. Only the door latch to make and fit and then onto designing a grate. Not sure to make 4 piece removable or fixed with hinge down centre part. The former will allow complete cleaning of the ashpan with a vacuum cleaner and brushes, the hinge down one will be fewer loose parts but the fixed sections each side prevent full access to the shallow 'wings' of the ashpan for complete cleaning.
At least it still fits, although there is some distortion I need to take out for a better fit.
And the hinged door being fitted.
Hope to finish off the ash pan tomorrow and scheme out the grate.
Chris D