Hi Phil,
I will post it here for all to see!
I have been writing for a good few Hours
and have come up with a lot on the first few subjects.
I still have Valves and Timing, Pistons and Oiling to go but here's what I've done on these subjects...
Incidentally my boiler number is 93 not sure how earlier this is, but does seem to lack some of the Winson modifications I've read about!
Here goes Part 1!
You may to want to print it!
Problems so far….FittingsI was not impressed with the brass chunk style fittings and valves so all have been replaced, as well as the site-glass due to its unacceptably small length of visible glass.
The safety valve was also unimpressive, not for its functionality as it does its job well, possibly to well at times. It is very harsh with a ‘pop’ action which makes you jump even if you know its coming, it also likes to empty the steam at an excessive rate on occasion with out closing off quick enough.
Mine has been replaced by a much ‘nicer’ one made by Dave Noble.
The pressure gauge did its job but was also replaced with one that went higher then 100Psi, as with a running pressure of 90 it didn’t give much indication if things went a bit ‘wrong’, plus it gives a better indication as 90 is actually printed larger, rather then having to marked on with pen!
I will talk about the regulator later….!
Boiler LevelThe boiler was not level in the frames and was rectified by jacking the firebox end up about ¼”.
This is simple enough, but this then means the spectacle plate( front of cab) is now to big meaning the firebox profile of the plate needs filling down to allow for the extra height.
As well as this the strap across the top of the boiler between the two tanks is now to short, so a new one has to be made. Adjustments tot eh front of the tanks has to be made with a file to try and complete the curve of the boiler at its new height, this is tricky as the curve of the tank did not match the curve of the boiler to begin with!
Smoke Box and Blast PipeThe original builder of my 1400 already noted the problems with the blast pipe alignment with the chimney and has attempted to rectify this by cutting and soldering the exhaust pipes to a vertical angle (when screwed into the pistons). This is due to the pistons being on a downward angle and the pipes having to screw directly into this meaning the pipes and the joining single blast pipe point at the same angle as the pistons away form the chimney.
To get a good straight up the chimney angle the smoke box needed to be moved (!). This was the easiest approach to resolve the miss alignment problem and only involved pushing the sealing ring on the back as far as it would go. Once pushed back the smoke box was drilled for a new securing bolt and refitted giving an almost direct aim up the chimney! The movement couldn’t be more then 2 or 3mm back so aesthetically I don’t think anyone would notice, especially as a lot of the other bodywork as mentioned before isn’t spot on!
I have also narrowed the blast pipe to aid draw on the fire, this has only been narrowed by a couple of thousands of an inch using a very small length of copper tube. The results are very encouraging, giving a very obvious aid to steaming and change in exhaust note!
Leaf SpringsBrass and tufnol.....very springy!, er no, both my rear axle leaf springs have been remade in spring steel to give support on the rear after simple bending under any weight. Initial running of the loco had many problems including this one where the loco would frequently get board of going round the same piece of track and would jump off at the front on each curve, this being quite scary when on raised track!
Now with all home baked steel springs the rear weight is support keeping the loco level and weight on the front wheels.
The Regulator (This is a long one!!!)The original Winson design was never really spectacular, but does its job. The original builder of my 1400 decided not to go with this, although I’m not sure why as his even more unspectacular design was rather nasty. It was a not very well made screw valve with thin pipe work and loose ‘slap around in the boiler’ style steam intake pipe up into the dome. After getting fed up with the loss of steam from the valve not closing properly I investigated the probability of integrating the new Modelworks regulator into my boiler.
Seeing as though Modelworks were basically rebuilding the Winson model but upgrading and entirely redesigning some parts of the model fitting new bits on to the old design, I thought it shouldn’t be too hard!
Looking at the regulator parts of a friend of mine who is currently building a Modelworks 1400 I came to the conclusion that the most important threads (the banjo bolt in the smoke box and regulator on the back plate) were the same and that if I could buy all the parts in between the two ends of the boiler the system should work.
Having already spoken to Modelworks about the sizing and fitting of the regulator into a Winson boiler and having them confirm that they thought it would be possible as they ‘are the same’.
So I ordered the entire Regulator system (let me know if anyone wants to know the exact bits) and waited for it to arrive…
After arrival and faffing around for a while looking at the bits and comparing sizes etc, I put the large regulator assembly in the hole in the top of the boiler and it fitted perfectly… that was until I pushed through the regulator rod from the back plate and attempted to mate the two together in the boiler.
This is the conversions Only downfall…
After more faffing and jiggery pokery I managed to get the hex end of the rod into the regulators hex socket, but there was clearly a major problem in height difference.
It turned out that the regulator mechanisms had to sit about 7mm higher in the Winson boiler to mate successfully with the rod, this means that the mechanisms sticks out the top of the boiler and is not supported as it only has air and the bendyness of the rod to sit on..
Screwing in the steam collector tube and banjo bolt from the other end confirmed this height difference. The mechanism worked perfectly except for the fact that I couldn’t seal the boiler with the inner dome cover anymore!
I investigate the height of the regulator in my boiler and came to the conclusion that the new Modelworks regulator was obviously sitting lower in the new boiler, although the banjo bolt at the smoke box end was at the same height as mine!
At this point I was extremely disappointed and was immediately on the phone to Modelworks to tell them about this problem, so if anyone else wanted to try this that they would need to do what I figured out I would need to do to make it work…(!)
More measuring and bad comparison drawings of the dome and inner dome came up with the answer that if I was able to make/get a brass ring the same diameter of the regulator hole and around 7mm high I would be able to raise the height of the boilers regulators hole to support the mechanism! The comparison and area drawings of the dome and inner dome showed that because there was so much material left in the dome I could get it machined out to fit the increase in height with out making any difference to the locos aesthetics!
Kricky, I’ve written a whole A4 page worth on this, if your still reading, Thanks!
Anyway, I was back on the phone to Modelworks and asked if they could make me a ring as described, the answer was yes…
MONTHS later after lots of phone calls and what I was told to be a Royal Mail delivery problems one turned up and even though this time one was supposedly sent by recorded delivery and one by normal delivery which one turned up… the standard packet!, god knows what was going on there, but anyway I finally had one and some gaskets all for free!
Taking a closer look I found the ring was in fact a standard ring made for the top of the boiler so it was perfect size, it even had the holes drilled in for bolting the dome cover down! After some non precision engineering style sanding/machining I got the ring down to around 6/7mm in height and nice and flat, don’t ask me how as you don’t want to know!
I was almost there, I fitted it on with plenty of gaskets and black paste, screwed and sealed everything else into the regulator system and finally bolted down the inner dome cover.
Finally after about 5 months of waiting and faffing from removing the old regulator it was done and apart from some fettling of the valve and arm alignment it was ready to test.
Now after some good amount of steamings it has proved to be very successful, sealing off properly every time with no steam leaks anywhere along the system and very user friendly, although it does need a bit getting use to at first as it can be very sensitive!
I will post some pictures if anyone is interested!
Part 2 will be posted soon, possibly tomorrow,
Happy Reading,
Steve